The Journey Begins

Let me introduce myself: I’m a long time geek working in the computer industry on open source software. I spend too much time in front of a computer. Way too much time.

I needed to do something to get away from the computer. Something physical – something to get dirt under my fingernails and sore muscles. Something where you can actually touch and see results at the end of the day.

So I decided to restore a car. [Insert scary music here]

Note: while WordPress puts the most recent posts at the top, you can also read the story in order starting with The Car Shows Up.

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We Aim to Please

Another entry in the list of places where I have outsmarted myself trying to improve things…

When I got the Imperial the rear springs were sagging a bit. As part of rebuilding the rear suspension I replaced them with new springs – along with replacing all of the suspension bushings, new shocks, and adding a rear sway bar. I had a choice on the springs: standard or heavy duty. Well, heavy duty is better so I ordered that!

The new heavy duty springs raised the rear end significantly. Producing two side effects: first was causing a mis-alignment in the drive shaft. On older Imperials this is known to produce a noticeable vibration on acceleration between 25 and 30 mph. Yup, I’m shaking. Badly. I’ve removed one leaf from the springs which helped. Really need to take out another leaf but this is a difficult job I’ve been procrastinating on. Driving the car has made the situation better as the suspension pieces settle in and this problem is almost gone. Guess I’ll keep driving and see if it goes away completely.

The second problem is that the headlights are pointing down at the road giving you what seems like ten feet of light in front of the car. Nowhere near enough light for safe driving!

I upgraded the standard sealed beam halogen lights that came on the car with a new set of Hella headlights that use modern H4 bulbs. These Hella headlights are direct replacements for the old style 5-3/4″ sealed beam headlights, get good reviews, and have a much better light pattern than the old sealed beam headlights. They are also significantly brighter.

I really wanted to go with a set of Holley RetroBright LED headlights which are modern headlights that can be installed on old cars. They are fully street legal, unlike many of the cheap LED headlights you can buy online. The Holleys get great reviews and look like the way to go. Unfortunately they are $200 apiece. The Hellas, on the other hand, are under $200 for a pair. And I probably won’t drive the Imperial at night that much…

Knowing about the aiming problem and considering how sharply down the headlights were pointing I really cranked the alignment setting up when installing the new headlights. I used the brute force method of turning the headlights on and adjusting the beam against the toolbox on the back wall until it looked good.

Which brings us to a couple of days ago. I finally decided to fire up the Imperial after dark and check out the headlights. The Hi beams (old headlights) were still pointed down into the road. The Lo beams (new headlights) were doing a great job of lighting up the tree tops. Yeah, other drivers are really going to like that…

The good news is that, on average, the headlights are aimed properly!

Last night also got dark (amazing how that works!) so I headed out to the workshop. Measured to the top of the headlights and marked that on a yardstick with a piece of tape. Set the yardstick up in front of the headlights and turned them on.

The new Hella’s have a great pattern – very sharp horizontal cutoff to the left to avoid blinding other drivers and a rising cutoff to the right to help you better see things. And the cutoff was well above the height of the headlights meaning that they were pointing up. Yeah, not good.

I adjusted the aim so that the cutoff was an inch or two below the tape. Then moved over and adjusted the other Lo beam. Head out around the block and see how this adjustment is.

Much better! I can’t see the treetops as well and the light cutoff on the left side is providing reasonable range and doesn’t seem to be high enough to bother other drivers. Visibility to the right is better, but doesn’t go as far as I would like when turning corners. Hi beams are a mix – good from the Hellas and the old headlights still point down.

Back into the shop and tweak the adjustments. Turn the passenger side Hella farther to the right. Adjust the old headlights so that their beam is closer to the tape mark – these headlights have a much rounder pattern so this adjustment is more approximate.

Head back out on the road and admire the headlights. The low beams provide good visibility. I’d like to have them brighter so looking into some high output bulbs. Bulb choice is one of the reasons for choosing the Hellas – any H4 bulb will work in them. Including the 100 watt “off road only” bulbs. Well, there are also a number of legal choices to try.

The Hi beams are great – they really light up the road!

With things checking out driving around the neighborhood it was time to take a longer drive. The good news is that I can see much better now. Not as good as the headlights in modern cars but entirely usable. Even better none of the other cars are flashing me – a good sign that the headlights aren’t blinding them.

Now there is no reason to fear sundown!

Update:

I went ahead and ordered a set of Sylvania 9003 SilverStar Ultra High Performance Halogen Headlight Bulbs – these got good reviews as one of the brightest bulbs available without getting into the 100 watt offroad lights. They are noticeably brighter than the standard H4 bulbs.

Got in a good night time drive – headlights are working well. The instrument panel is easy to read and the HVAC push buttons are clearly lighted. Life is good!

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New Toys. Errr… “Tools”

So I was perusing CraigsList…

That introductory line is right up there with “hold my beer” as an indicator that things are about to get interesting!

I’ve been wanting a specific set of tools to expand my sheet metal fabrication capabilities.And here was a listing for the four tools I most wanted. For $200 for the set. Road trip! Well, if you can call 40 miles a road trip…

Bead Roller

A bead roller is used to put various types of grooves and raised areas inside sheet metal panels, usually for stiffening. It can also be used to put flanges and raised sections on the edge of a panel, and is one of the few tools that can handle curved edges.

Bead Roller and wheels

English Wheel

An English Wheel is a specialized piece of equipment that produces smooth curves in two directions. In the hands of an expert it can produce amazing shapes with great accuracy. I’m no expert but I did learn the basics of using an English wheel in the coachbuilding course I took a couple of years ago.

Shrinker/Stretcher

The basic use of a shrinker/stretcher is to allow making curves in flanges. The most widely used alternative is to cut pie shaped wedges in a flange and then curve it. In many cases you then have to weld up the gaps in the flange which is a lot of work. A bead roller and shrinker/stretcher would have been a big help when working on the Imperial doors.

Bench Shear

A bench shear produces highly accurate cuts in sheet metal with little distortion for both straight lines and curves. You feed the sheet metal through the shear allowing long cuts.

A bench shear is easier to use and more accurate than aviation snips, faster and often more accurate than sawing, and produces far less mess than using a cutting disk. It is extremely fast requiring no setup – just draw lines on the sheet metal like usual, feed it into the shear, and pull the handle.

Once I get this shear mounted on a workbench it will really speed up working with sheet metal – I’m looking forward to it!

Now to find a project where I can use these tools!

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Electrical 17: Chasing Gremlins

I’ve had an intermittent electrical problem for several months – one of the most frustrating things that can happen. The courtesy lights – lights in the front doors and a map light in the dash – come on when you open a front door and go off when you close the door. At least they are supposed to…

The problem started last spring when the courtesy lights came on with the Imperial just sitting in the workshop and then completely drained the battery. Fortunately I was able to recharge the battery and it seems to be OK.

I started to trouble shoot the problem and it went away after driving the car. OK, yet another reason why you need to regularly drive your cars!

Since then the problem has randomly occurred and then gone away. Finally last week the lights came on and stayed on. Great! A hard failure can actually be diagnosed! And it was a good time in the project where nothing else was in the way. Time to dig out the multi-meter and patch cords and see if we can chase this gremlin down!

The first thing to know about lighting circuits like these is that they are wired up backward. Most circuits switch the power on and off and have ground permanently connected. This can get complicated when you have multiple switches and multiple lights on a single circuit and require multiple wires to make everything work.

On the other hand you can permanently provide power to all devices and have the switches connect to ground. Any place you close a switch, completing the circuit from power to ground, all of the lights on the circuit will come on. Simple, elegant, and effective!

I’ve been suspicious of the door switches. These are 60 years old and subject to wear. It would be easy for these to start making accidental contact to ground.

Starting with the drives door I manually worked the door switch. The initial signs were encouraging: Off then on, off then on. But then it went Off then on, off then on, off then on, on, on, on – even with the door switch physically removed from the circuit. OK, apparently not the driver door switch.

Next the passenger door switch. Once again the initial signs were encouraging: Off then on, off then on. But then it went off then on, off then on, off then on. Looks like we found the problem, so put the trim panel back on. And admire the now shining lights. That are supposed to still be off.

This actually makes sense! Looks like there is a short in one of the wires. Take the trim panel back off and the light goes off. Carefully examine the wires. Hmm, can’t find anything; the wire looks fine. Put the trim panel back on the the lights come back on. Take the panel off and the light goes out.

Just a minute – if I wiggle the wires in a different place the lights come on! OK, maybe there is a short circuit someplace in the middle of the dash. But these wires also look good. And now I can’t get the lights to come on.

Put the trim panel back on and the lights come on. I’m now getting both annoyed and frustrated.

While pondering the situation I hit the electric window button to make sure that the power windows still worked. The window worked great, instantly dropping down a couple of inches. And the lights went off. Raise the window back up and the light came back on. Ok, this is interesting. Try it some more: down/off, up/on, down/off, up/on, down/off, up/on.

This is a strong indication that there is a problem with the wiring inside the door! It looks like the window is rubbing on something and creating a short circuit. It is going to be a pain to open up the door and work on the wiring inside the door, but at least there is something solid to go after.

The first step in taking the door apart is to remove the light fixture from the door. And maybe I will get lucky and the problem will be close to the fixture so that I can fix it without taking the entire door apart.

Remove the chrome plated metal fixture from the door and the light goes out. OK, it really looks like a wiring problem! Play with the wiring for a while; nothing obvious. And the light doesn’t come on.

Put the fixture back in the door to check how the wiring fits. The light comes on as soon as the metal fixture touches the metal door. Try it several times and get the same result.

This is odd! Many light bulbs are grounded through the shell and this would be expected behavior. But this bulb has two terminals – one for power and one for ground – and the shell of the bulb doesn’t do anything. Unlike most bulbs the shell isn’t electrically connected to the filament. It doesn’t make sense for the bulb to light up when you ground the fixture.

Pop the bulb out and carefully examine the bulb, the socket, and the fixture. Nope, don’t see anything that would create a short.

Except…

I had replaced some of the courtesy lights with LED bulbs for more light, less heat, and less power. Just some of the bulbs – the LED bulbs wouldn’t fit into some of the sockets. And this was one of the LED bulbs.

Could there be a problem with the electronics inside the LED bulb creating an intermittent short circuit to the shell? Perhaps a short that was temperature or vibration related? Could it simply be the wrong bulb for this application? Could I have (once again) out-smarted myself trying to improve things that worked fine before?

Dig through my stash of bulbs and find a standard 1004 courtesy light bulb. Install it in the fixture and then ground the fixture. Nothing! Open the door and the light comes on. Just as it is supposed to.

Re-install the fixture in the door. Open and close the door several times – the light goes on and off every time. Try the drivers door – the light goes on and off every time it is supposed to. Try the map light switch. The light goes on and off every time it is supposed to.

Grab and wiggle the wiring every place I can reach it – the light stays off. Try the doors and map light again. Everything works.

All of that work was yesterday. I went out to the car today and tried everything again. Still working like it is supposed to!

At this point the indications are that it was in fact a defective LED bulb. But I’m still going to keep a close eye on it for the next several months. And I probably won’t be “upgrading” any more lights to an LED without a good reason!

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Electrical 16: Heater Illumination

The Imperial uses electroluminescent lighting for the instrument panel, heater controls and transmission controls. The heater and transmission use plastic pushbuttons with a panel beside them to light the button caps. Unfortunately these panels degrade over time and now barely illuminate the push buttons.

Further, after re-connecting the panel for the heater controls the overall illumination for the instruments is excessively dim – and I’m someone who turns the instrument brightness down to where they are barely legible!

While contemplating this situation inspiration hit with an audible thud – “hey, don’t they make LED panels? And LED dimmers?”

A quick search turned up a set of 2″ x 2″ LED panels. Available in packages of 10 for $15. And dimmers for LEDs are around $10. OK, this is cost effective! At this price I can afford to experiment.

So I ordered a set and tried them. The work great! Amazingly bright on full power yet able to be dimmed to almost nothing. This should work!

That was two years ago. Getting the heater control out is such a miserable job that I put this project on the back burner until I had another reason to pull the heater control. That day finally arrived – I’ll make another post on that little incident..

With the heater control on the bench I discovered that three of the LED panels nicely covered the illumination plate. And three panels work just as well as a single panel on the dimmer.

Heater control with LED panels installed on electroluminescent panel

With the heater control installed back in the dash (first of many times. sigh.) it was time to connect the LEDs to the dimmer. And to connect the dimmer to a power supply.

LED test

It would be really nice to have this in the headlight circuit so the the heater lights are turned on and off with the rest of the dash lights. But all of the instrument lights are plugged into the back of the instrument panel and totally buried. The power for the original electroluminescent panel is 200V AC – won’t work. I had been postponing this part of the project for multiple reasons!

Hmm, there is the unused connector for the radio backlight… (The radio is another “interesting” story that I’m trying to block out of my memory.) It has power. And dimming. I wonder if the LED and dimmer work with less than 12V input power? Time to make a temporary connection and find out.

Well – would you look at that! It actually works quite well with the dash lights turned down low! The max brightness is less than you get with the full 12V, but even with the reduced input voltage I need to dial it way down.

LED off (left) and LED on (right)

I’m going to declare this one a success!

Previous Electrical Post: Electrical 15: Factory Wiring Diagrams

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An Air Conditioning Thread Pull

You know when you have a sweater with a thread hanging loose and you pull on it? And you keep getting more and more thread until your former sweater is nothing but a pile of sheep fur on the floor?

I decided it was time to get the air conditioning charged again and see if I could make the Imperial even cooler than it already is. Something about a black car and the hottest July on record.

First order of business: flush out the AC evaporator, condenser, and hoses with AC flush. This went fairly smoothly and flushed out less crud than expected. OK, that’s a good sign! Call the garage and schedule the re-charge.

One of the idiosyncrasies of the new generic heater control is that it engages the AC compressor clutch when selecting MaxCool, Cool, or Heat. The temporary expedient was to unplug the compressor clutch over the winter. So I needed to plug the compressor clutch back in. And check to make sure it still worked. As you probably guessed, nothing.

Well, dogbreath!

First question: is it the clutch or the wiring? Hook up a temporary jumper to the clutch, connect it to the battery, and be rewarded with a solid clunk of clutch engagement. OK, wiring it is.

Next, check the fuses and make sure that power is going to the heater control. Yup, power is good at the fusebox. Sigh… Nothing left but one of my most dreaded jobs – remove the heater control!

Remove the glove box. Remove the ash tray. Remove the right hand defroster vent and hose. Remove the radio. Now start blindly reaching into the back of the dashboard to unbolt and remove the heater control. Yup, buried just as deeply as it used to be. Yup, just as awkward to get to as it used to be. Yup, just as many sharp edges in there as there used to be. Yup, I still have trouble finding things by braille.

With the heater control finally out, wipe the blood off and start electrical trouble shooting. Hmm, no power to the clutch circuit. There was a similar problem last time. Fine, be that way! I have plenty of spare power circuits in the new fuse box, so just run a new dedicated power line directly from the fuse box to the heater control.

Try the compressor clutch again. This time I’m rewarded with a solid clunk when I push the button. Out of paranoia check the fan (which is the other part of the heater control): low, medium, and high, check. And the new LED lighting panels work (separate post on that). Reinstall the heater control. Check that everything is working. Still good!

You know, I should probably check the power antenna switch while the radio is out since the radio completely blocks access to this switch. Hmm, only goes down… OK, dig out the factory service manual and check the wiring. Three wires: power, up, and down. Of course the wires are different colors on both sides of the connectors…

Grab the multimeter and check all three wires. OK, this wire has 12V on it, so it goes to the center of the switch. The other two wires go to the other two connectors. And the antenna now goes up as well as down!

Reinstall the radio. Wrestle with the defrost vent and hose until they cooperate. Reinstall the ash tray and glove compartment and then sit back and admire a difficult job completed. Just to be sure, check out the compressor clutch and the fan. Satisfying clunk from the compressor, and fan works on low, medium, and… No high speed on the fan.

Well, carp! I can’t leave it like that.

Pull everything apart and start checking with the heater control now hanging under the dash. Everything works… OK, maybe a loose connector? Re-seat all connectors, re-install the heater control, wipe off the blood, and check. Everything works.

Re-install the radio. Check everything again before going any further. No high speed on the fan.

Pull the radio out. Check the fan. Works on Low, Medium and Hi.

What the freaking Hades is going on here?!? There is NO connection between the radio and the heater control. There is no way for the radio to interact with the heater or fan. This physically cannot be happening!

Pull everything apart. With the heater control hanging under the dash test all functions. Yup, with the radio removed the fan works on Hi.

As an alternative to an exorcism of the car I dragged out the wiring diagrams and multimeter and started tracing and checking each part of the heater circuit from the fusebox all the way to the fan.

Hmmm, this is odd.. This connector near the fan feels like it has a broken wire. This is a butt connector covered with heat shrink tubing that should be one of the most solid and reliable parts of the entire circuit. And, of course, it is on the high speed circuit. This part of the wiring harness goes from the heater control, under the radio, and to the fan. Where it would be moved and jostled when installing the radio. No, no – this is just circumstantial evidence – don’t jump to conclusions!

The usual test is to tug on a wire and see if it comes out of the connector. This doesn’t work when marine grade heat shrink tubing glues everything together. The situation is suspicious enough that it makes sense to just cut the connector out and replace it.

With the old connector cut out might as well take it over to the workbench and slice off the heat shrink tubing to check the wire. Yup, damaged wire and a bad crimp. Moving the wire would make and break the connection. This evidence is more than just a smoking gun – it is like having surveillance video of the crime scene! The worst part is that these wires are new – I made them as part of installing the new heater motor. Yup, the usual idiot is to blame.

Double check and triple check the crimps when installing the new connectors. Make absolutely sure they are solid this time.

As part of the detailed trouble shooting I reviewed the heater control switches. I had wired the new switch just like the original factory switch, which meant (with this new universal switch) that the AC was running when heat was selected. Connect it differently and AC only came on for Cool and MaxCool, so I went ahead and hooked it up that way.

Check all functions — all good. Re-install the heater control. Check all functions — all good. Re-install the radio. Check all functions — all good. Re-install the defrost hose and vent. Check all functions — all good. Re-install the ash tray and glove compartment. Check all functions. Wait for it, wait for it…

All good! Not there yet – fire the car up and take it for a test drive. Check all functions — all good.

OK, I’m getting cautiously optimistic.

The AC recharge is now scheduled for next week.

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Front Seat Finished!

Unfortunately we aren’t done yet. Three back panels are required – two sides and a center piece. These panels fit around the mounting brackets for the seat back and arm rest. Unlike the factory cover, these will be seat material instead of carpet. Each panel is measured, cut, sewn, test fitted, and then sewn to the cover.

Finally we are ready to fit the entire cover. With some pushing, pulling, tweaking, and cursing the complete cover is in place and looking good. Flip the seat over the use hog rings to secure the seat cover to the frame. Then flip it back upright and check the overall fit. Not bad, not bad at all! Since everything is in its final position, cut out the holes for all of the mounting points.

Being thoroughly paranoid at this point, the complete seat is assembled – arm rest and seat backs – and the whole seat is checked over for any last problems. Everything still looks good…

Time to take the seat back apart, drag the engine hoist out of the corner, hook everything up, and call She Who Must Be Obeyed.

The seat base went back into the car smoothly. The mounting bolts slipped into their holes in the bottom of the car – everything still fits. Run the nuts onto the mounting bolts and tighten everything up. The next moment of truth – plug in the power seat and see if it works. It does! It moves in all six directions. So far, so good…

Install the arm rest with its cover. Install both seat backs. Install the trim pieces on the sides of the seats. Everything is still looking good.

Now for the real moment of truth – run the seat back to its correct position, slide in, and sit on it.

Wait for it, wait for it…

It is good! The seat is now firm and comfortable. There is much better support and it doesn’t feel squishy. It even looks good! And there was much rejoicing!

New front seat

We’re not quiet finished – the front door cards still need to be done and I need to do some tweaking around the windows. But the car is usable and even looks good. We may eventually get a Thursday that isn’t raining so I can take it to the local car show!

I’ve been working on the interior more or less non stop since the first of February – three and a half months so far. The front door cards still need to be done and there is some trim work left to do. And the success on the interior has inspired me to consider some additional projects – yeah, potentially a bit of foreshadowing. The car is ready for the road, so I really should spend some time driving it instead of working on it. I sometimes forget that this is a car to be driven, not just a never ending money sucking series of projects on a static display… That this is a vehicle, not an art project!

She Who Must Be Obeyed has graciously reminded me that some projects on the house need to be worked on, so I’m going to shift gears for a while. But I’m happy with where the car is now!

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What Now?

Today is a new day. Returning to the debacle of the seat cover that doesn’t fit the first thing is to cast aside all assumptions and do a systematic trouble shooting of everything.

The first thing I discovered is that the sides of the seat aren’t at right angles to the front – they are actually at 83 degrees, not 90 degrees. OK, that makes a difference. There is an inward jog at the back of the seat. OK, that needs to be included in the template

While the factory seat covers aren’t suitable for making templates they can give you a rough idea. Working against the seat frame I had made the corners with a 3″ radius. Looking at the original covers they had a much larger radius.

But how to make a large radius? Well, the drafting set I’m using (a professional set from my days as an aerospace draftsman) has an extension bar for the compass. Let’s make circles with radii from 5″ to 10″ , cut them out of cardboard, and see which one fits best. After trying all of them it looks like an 8″ radius is the best fit.

Taking this information we create a new template.

As long as we have the seat backs mounted on the base let’s mark the foam with the edges of the seat backs and the seat inserts. We can then use this to fit the top seat cover and precisely locate the seat inserts and center panel.

Seat back alignment marks

With this information we can position the seat inserts, add filler strips on the outside edges, and determine the exact size for the center panel between the inserts.

Based on the new template I was able to save and re-work the seat inserts – all other pieces had to be discarded and done from scratch. This wasn’t completely bad – the inserts required the most work to make so I was glad to be able to use them. All of the other pieces were simply cut out and sewn together.

The new template is used to mark the outside edges and the radius for the corner. This corner radius goes into the insert, so the insert is trimmed to fit. After the entire top panel is sewn together it is draped over the seat base and test fitted.

The front and sides were made using the original front and sides as templates. Despite the problems with the first seat cover these pieces seemed to fit OK, so we will use the same templates to make the new ones. To correct the problems with the seam we sew the front and side panels together and pin them in place on the seat base and foam. We then use the edge of the side and front to mark the top panel, add seam allowances, and mark this on the top panel. Hopefully this will give us a consistent seam around the entire seat rather than one that dips around the ends.

Taking a deep breath, sew the top and sides together. With considerable trepidation test fit the new cover.

And it fits! Maybe not perfect, but much better than the first cover.

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Not Acceptable

Encouraged by the results so far I started working on templates for the seat cover. Unlike the rest of the seats, I wasn’t able to use the original front seat covers to make templates. The front and sides were OK, but the top was just too messed up to use.

No problem! All that I need to do is make a template from scratch. Dig out the construction paper, take measurements from the seat frame and foam, lay it out on the paper, cut it out, and lay the paper on the seat. Yeah, that looks pretty good!

Transfer the template from paper to vinyl, cut it out, sew it together, and fit it over the seat.

And it fits like crap. Very loose corners which just can’t be made tight no matter what I do. Both front corners and back corners don’t fit. The seams between the top and sides droop badly where they should form a consistent line all the way around.

After trying everything I could think of to make it fit the realization slowly crept in: this just wasn’t going to work. It wasn’t acceptable. I couldn’t live with it. For the first time on the interior work I had done something that was bad.

Trying to fix this mess while frustrated and tired is a prescription for making things worse.Turn everything off, lock the door, and come back another day.

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Re-Foaming

I’m not happy with the replacement foam on the back seat. I need to do something better for the front seat – after all, this is where I will be sitting! OK, drag out the new foam, cut it over size, plop it on top of the seat frame, and start studying the situation.

The challenge is how to wrap it over the edge of the seat frame and have it hold its shape. The soft foam previously used on the front seat wrapped over the edge easily; it provided no guidance.

Unlike the seat covers you can’t use hog rings to secure the foam to the seat frame. There isn’t enough surface area on the seat frame to use contact cement. Welding is out – I didn’t even try. Maybe loop rope or cord through the foam and around the frame?

Just a minute – what about sewing the foam to the frame? All of my sewing has been using the machine which clearly won’t work here. But what about old school needle and thread? I have plenty of heavy thread. But what about a needle? Just a minute – they make heavy duty needles for sewing things like carpet and leather! Would that work here?

It turned out that She Who Must Be Obeyed actually had a package of heavy duty needles which she graciously allowed me to use. Let’s do this!

Trying the novel approach of thinking before acting I realized that the foam was likely to move when I started wrapping it over the front edge of the frame. OK, just start by sewing it to the back of the frame first. Trying a few different approaches I discovered that the large needle easily penetrated the foam and that it was better to do a separate loop for each connection to the frame rather than trying to sew a seam.

With the back secure I tackled the front, starting from the middle and working out. Wrap the foam over the front of the frame, select a point on the frame to loop the thread around, and knot it in place.

Not so fast! I can’t seem to hold the foam securely in place while running a needle through the foam, around the frame, back through the foam, and tightly knot it. If only there were some way to clamp it in place… Oh, wait – I have clamps!

Front Seat Foam clamped in place before stitching

Well, would you look at that! The foam is actually wrapped nicely over the front of the frame and ready to fit and secure the cover.

Front Seat Foam wrapped around edge of frame and stitched in place

The next question is whether or not the cover will work. The first check is to take the panels and drape them over the seat to see if they look like they will fit.

Test fit of seat cover panels

A really rough fit of the cover panels is encouraging – it looks like this will fit after some trimming and adjustment.

I can’t be sure until the job is done, but it looks like this is going to work!

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Front Seat Base

Good thing this was saved for last – the base of the front seat was trashed! Once the aftermarket covers were removed you could see that the factory covers were completely shot – worn out, shredded, stretched, and basically horrible. The factory foam was completely missing; this is the one place where they had completely replaced the factory foam with new foam. And they didn’t use automotive foam – they used a regular foam that is quite soft. This would explain why the front seat never felt right and why it had such poor support!

Front Seat Base
Front Seat Original Cover
Front Seat Foam

This is going to be a job. I need to replace the foam as well as the seat covers. I don’t know why Chrysler used carpet on the seat base as well as the door cards, but I hate it – that has to go!

Wish me luck – I suspect I’ll need it…

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