A Juki Roller Coaster Day

Having achieved an almost acceptable test panel with the junk vinyl, I decided to make one last test panel. This last test panel would use the actual vinyl I will be using for the seats. I also needed to change thread from the cheap Amazon thread I’ve been working with to the good thread for the actual seats. And this is probably a good time to change the needle.

The first step was to fill up several bobbins with the good thread and swap in the new bobbin. Then thread the good thread through the machine, using the old thread to pull it through to make sure that the machine was threaded properly. Next, change out the needle. Finally, make a quick test seam to verify everything, and start working on the final test panel.

The result was immediate disaster. Seams completely open on the back. Seams with the stitches very loose on the back. Not Good! Time to start troubleshooting.

Hmm, it looks like I installed the needle backward. OK, rotate the needle to the correct position and try again. This time I’m getting stitches, but they are very loose. That looks like the tension setting needs to be adjusted. Spend the next hour or so changing the tension adjustment to both tighter and looser with very little change.

With frustration rising it was time to walk away. Well, it was lunchtime. Grab a sandwich, fire up the Internet, and start researching the problem.

With a list of things to check, head back to the machine and return to pounding my head against a brick wall. After chasing several more dead ends, I started studying the threading of the machine. I knew this was good, since I hadn’t changed anything and had used the old (working) thread to pull the new thread through the machine.

Just a minute – something doesn’t look right here… In fact, if you look at it closely… It looks like the thread has jumped off of both of the tensioner disks. KRUD.

Pull out the user manual, study the section on threading the machine a dozen times, and thread it according to the instructions.

Grab another scrap of vinyl and run a test seam. MUCH better, but not perfect. OK, start adjusting the tensioner. This time it makes a noticeable difference. After a half dozen seams the machine is dialed in nicely.

Take a scrap of the seat vinyl, which is much heavier than the test vinyl, and run a test seam. Good, but not quite perfect. A few small adjustments of the thread tensioner and it is sewing perfectly with the seat vinyl.

Yup, as usual, the one thing that you know can’t be the problem is what bites you. Yes, further confirmation that I’m an idiot.

Now, I can finally cut out the pieces for the test panel using the actual seat vinyl and sew them together.This heavier material has a different feel, but I was able to achieve a successful result.

Final test panel

This panel is actually better than it looks in the picture – as soon as it is stretched all of the wrinkles disappear. After a roller coaster day I think I’m ready to start working on an actual seat.

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